This is not a conversion kit. It was built from scratch for a 39 chevy.The MC is an aftermarket "street rod style" and the booster is a standard 7". I think I had the front and rear lines crossed from the MC to the proporting valve so I changed that and nothing different happend. The proportioning valve has a built in metering valve and I am 100% the plumbing is correct. I am using a DOT 3 fluid in the system.

Everything is functioning now that I got rid of the front 2# residual valve. I still have the rear 10# in there. The system works great great under no vacuum but once I start the car, I have a long pedal throw. I think that is a simple pushrod adjustment or some air in the lines though.